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How to make your Athearns run!
"Detailed analysis & instructions for making your Atherns run."
by Moe Mechling
I always thought that the gods of remotoring were
wrong. I said before I spent a wad on motors, let me strip a loco
and see what is wrong. The motor out-used .3A. That meant 1A was
in the gear train. The motor draw wasn't too bad, it could be better.
I tore it down, cleaned and beveled the commutator and smoothed
it up. I put a .015 KD washer on the shaft, reducing the end play
to .010. I could have balanced the armature but didn't. It drew
.2A, which was within acceptable range and 1.2A in the mechanism.
Now I knew it was in the mechanism, and no motor change could improve
it. I worked on worm end clearance, bearing fit to the metal frame.
Just checked everything for several hours. Head scratching. Then
I got sore and finally I found a piece of heavy SQ plastic, took
the bottom cover off, and ran the loco. I couldn't believe my eyes.
The idler gears under worm and between drivers would fly back and
forth on the shaft. The casting taper and the taper inside the gear
opposed each other. Assembled that way to cut down play. Each time
they came to the end limit they cocked sharply and buried their
teeth into the other gear roots making a bind. That's eight times
an axle revolution. I found out that the casings had different shrinkages
depending on the operator's dreaming, the bosses shoe or quitting
early for a hot date. First I matched the gear taper to the stud
taper. Then the two axles were put in and two KD washers and gear
on the stud. The combination will vary; two .015 or one .015 and
one .010, or two .010's. The idea is to get both idlers as near
to level with the drive axles in the stud side of the case. Put
one washer on top of the idler stud and close the case. Too tight,
put an .010 washer on top. The case held closed, the gears should
roll over smoothly, with just a hint of side play. Checked with
a feeler gauge it should have .004" to .006" clearance. I put the
cases back together and it drew .25A!! Fixing that gear box assembly
reduced current draw by .95A, and 1.05 over all.
The total cost was 13 washers @ about $0.26. The
new Athearn mechanisms have straight posts and gear bores but still
need one .010 washer and motor end play checked. The old wide body
F units need worm end play checked. This needs .004-.006 end play.
I would tend towards .006 for the worm.
The final problem we didn't find until we put the
receiver in the rear loco and pushed a dummy ahead with the sound
unit. We hit blank sound over some switches and double crossovers.
I found out that the metal interior side frames holding the wheel
bearings had some kind of coating on them. Where the brass rivets
crimped through they didn't always make contact. They are also almost
impossible to solder as is. I took my flexible shaft with a SQ ended
carbide 3/32 moto tool burr and ground along the inside of both
rivets out about 3/16" and the joint to the motor pickup. Then I
sweat the three joints using Burnley soldering paste and 2% LMP
silver bearing solder (Radio Shack) the crook in the pickup is sawed
off the tab, ground, and tinned. A gold-plated .1 socket for motor
harness is sweat on each truck. This makes for easier maintenance
and the harness is fit with .1 Micro plugs to motor and receiver.
On the newer Athearn mechanisms there is a different set up. The
outer pate, plastic plate, and pickup are riveted together and you
must solder outside and the pickup plate inside the case.
The bottom motor retainer and spring clamp, pickup
we hammer the springs back up flat, solder the plug in front of
right side and put 2 pieces of plastic 4 mil. electrical tape inside
the frame.
The final problem was torguing or twittering while
running with the worm cover on the rear truck. Measure the space
between this and frame. Subtract about .005 as ACC has thickness.
It will fall in the .015-.020 range usually. Crown the pieces; cut
off lengths and glue to the bolster top. This eliminates the problem
and gives a three point suspension for track deviation.
To vent the body we use etched fans. Soak them in
acetone to remove from the backing tape. Cut them to dia and we
use a domed watch or clock glass to put the curve in. The cast fan
on the body is drilled and cut away to the last ring next to flange.
The fan blade ends are cleaned away with a graver leaving a flat
ledge. The grill inserted and glued in place.
On the side screens we use alum fence wire often
cut on the diagonal etc. The corners are drilled as shown with a
#1 counter bore in a pin vice. One end is worked out; the other
end freed. Trend Lines has a .010 x 40T saw blade that cuts on the
pull. Saw sides free, stay in back from the edge a bit and trim
with a knife and 4 cut 6" flat hand and jewelers files. Use a vernier
to get length and height even. Mark this down. Taper or bevel the
inside edge. Make a dummy plug of .040 ABs plastruct. Measure the
wire x 2 usually, .030, and make a plug .030 smaller than the hole.
We record the hole size and loco. Set the jig on a wire rectangle.
Bend the sides up with a 6" model rule, crimp the corners with pliers
and nip off the corners with scissors. Roll the rough corner with
a rule and trim sides and end to the jig thickness and remove the
screen pan. Push the pan in from the shell from inside use a rule
to get outside flush. Check inside that no wire sticks out to short
the receiver and ACC in place. Blot excess with squares of "Bounty"
kitchen towel. We do this all before super detailing the model,
after learning the hard way. Had a whole box of spare parts.
About 90% of Athearn frames are bent from casting
and shrinkage. It's easy to spot. Put a finger on both ends of the
shell and if it rocks up and down, it is bent. When you strip the
chassis out to work on the mechanism, put a wood block under the
end and tap with a hammer to straighten each end. Let it sit on
the tank. Check with a straight edge.
We saw the coupler tabs off the frame and build
up the shell inside for the coupler pads. Using #5 KD's almost exclusively.
Especially if a snow plow is on the front. The rear pad is too low
for #5 and too high for #7's, about .020 off.
"Toot toot"
"Mocn3" Mechling
NMRA 2711
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