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BLI SW7 Current Pulse Investigation
by Larry Maier, 03/05/05
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I received the GN 163 and C&O 5236 BLI SW7 engines.
Out of the box, both appeared to work on my layout. As I ran 5236
more extensively, I had frequent problems tripping the On Guard
breaker that feeds my layout. This happened particularly when I
reversed the engine while running. I was able to cure this problem
by using Deoxit on the metal bars that serve as the power pickups
from the main axles. My guess is that poor electrical contact may
have caused enough charging/discharging of the power supply capacitors
that too much current was drawn. After treating 5236, I was unable
to get either engine to trip the On Guard breaker by either normal
operation or by reversing the unit while running (not normally done).
I moved both engines to my workbench where I connected
a test track to a Digitrax DCS 100 with a DT100 throttle. I measured
the current drawn by inserting a 0.1 ohm resistor between the DCS100
and the test track. Both engines showed very high current draws
when reversed while running. The operating speed made little difference.
It appeared that as long as a speed step above 0 was used, reversing
the engine caused a large current inrush. The figures below show
typical results for each engine:
Note that the background fuzz in the
trace is actually the varying current drawn by the sound system.
These views show the the worst case observed for
each engine, but it is easy to see that the two engines are about
equivalent. I did the rest of my testing with GN 163. Reversing
an engine while it is running is a worst case scenario since the
motor rotating in the wrong direction acts as a negative
impedance and draws more current than it takes to simply start the
motor turning from a stop. I tried a normal stop (i.e. Speed step
= 0), reverse, start sequence and recorded the current when the
engine started to move. In many instances, there was no excess current
drawn. In some instances, however, I observed a significant current
draw at the start. Again note that for this test, I made sure the
speed step was 0 before reversing and starting the engine. I never
observed a current inrush during the reversing operation, but sometimes,
there was a current inrush when I started the engine moving after
reversing it. I did not observe the current inrush after the first
instance. In other words, I could start the engine any number of
times after the reversal, and only the first time after the reversal
showed the inrush, all other starts showed negligible current increases.
I should also note that I did not have a single DCS 100 shutdown
during this phase of the testing. The oscilloscope trace below shows
typical results from these tests. Note that the time scale is changed
from 10ms/div (above figures) to 25ms/div (figures below). The trace
below represents the worst case (i.e. the longest) transient that
I observed during these tests. Again, I was unable to cause a DCS100
shutdown at any time during these tests.
In an attempt to validate field reports of DCS100
shutdown, I added a fixed load of approximately 2 amps to the test
track. I then repeated the stop, reverse, start sequence. Under
these conditions, I was unable to demonstrate a shutdown of the
DCS100. I then tried a live reverse (reverse while the
engine is moving), and I was able to get the DCS100 to shutdown
and then re-start. Strangely, the shutdown occurred approximately
3 seconds after the start-up current surge from the reversed engine
and appeared to last for only a very short period of time. After
the shutdown, power automatically returned to the track, the engine
regained power, and the engine began operating in the new direction
at the commanded speed.
The oscilloscope trace below shows a typical DCS100
shutdown transient, although I was unable to capture the actual
shutdown.
Conclusion: It appears that there is a shutdown problem
only if the reversal occurs when the speed step is other than 0
(assuming good contact between the wheel axles and pickup shoes).
I suspect that there may be a software glitch for the QSI decoder
causing the problem?
A secondary contributing factor may be poor contact
between the pickup shoes and wheel axles as mentioned above. This
problem is easily cured by removing the truck side frames and placing
a drop or two of Deoxit D5 Power Booster (I know, pretty much a
marketing name) at the juncture of the wheel axles and pickup shoes.
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